Tezin Türü: Yüksek Lisans
Tezin Yürütüldüğü Kurum: Orta Doğu Teknik Üniversitesi, Mühendislik Fakültesi, Çevre Mühendisliği Bölümü, Türkiye
Tezin Onay Tarihi: 2005
Tezin Dili: İngilizce
Öğrenci: Devrim Kaya
Danışman: FİLİZ BENGÜ DİLEK
Özet:The objective of this study is to remove turbidity originating from algae present in oxidation ponds effluents by an easy and inexpensive method. For this reason, a novel lab-scale Step Feed Dual Treatment (SFDT) process was constructed and the efficiency of trickling filter (TF) to remove algae and organic matter was investigated. SFDT process developed in this study is the unique, inexpensive and new system to scavenge algae from oxidation pond effluents. In this system, influent is first treated in a stabilization pond, and subsequently they directed to a TF, so as to provide a dual treatment. Moreover, some fraction of the raw influent was directly sent to TF to maintain a steady biofilm on the TF medium. Stabilization pond was not simulated in the experimental set-up as the main objective of the study is to observe TF ability to scavenge algae from pond effluent. To determine the magnitude of the effect of individual operational parameters (hydraulic loading rate, influent COD and chlorophyll-a concentration) and of their combinations on organics and particle removal efficacy an experimental design was followed. Experiments consistent with twolevel factorial design with three variables (23) were performed. Hydraulic loading rate (HLR) (0.5-2 m3/m2.day), influent COD (150-550 mg/l) and influent chlorophyll-a concentrations (Chl-a) (250-600 æg/l) were selected as independent variables. The COD and algae removal (as Chl-a) were selected as dependent variables. Data obtained from the experiments showed that when HLR (m3/m2.day) was increased from 0.5 to 2, Chl-a, NTU, SS and COD removals were decreased, however, more than 85 % removal was attained in each case, except for COD. The lowest removal efficiencies were obtained for all the quality parameters when hydraulic loading was increased to 4 m3/m2.day. It was observed that in general removal percentages for